New Project - Skunkwerks EM9D
New Project - Skunkwerks EM9D
Quick update:
I went to the Dyno day yesterday, but with some mixed results.
I think I am having an issue with the head gasket, no oil contamination, but the coolant hoses are getting pressurized and it looks like I have some dark substance in the coolant tank It does not seem to have perceptable loss of power, seems the same as before. I also seem to be leaking from the heater core, I have a drip of coolant under the car near the transmission.
On the way to pick up my son the trans started to slip a bit in fourth gear...more on that later.
Got to the dyno shop and J-sauce was the first up. Dyno operator made acouple of pulls and he was only getting around 175 hp - runs were taken in 3rd gear. The operator made runs in 4th gear and his readings went up to 350+.
When it came time to my runs he could not figure out how to get an rpm output, I didn't know so I suggested to clamp on the tach cable, but that didn't work. Where is the correct point to measure RPM output?
So he made a run in 3rd and was low on the output, so he said he needed to be in 4th. I told him put in D and go. He says is down shifted and wasn;t going to work. I told him to wait until 60-65 and floor it.
He made his run, it sounded mean and not much smoke. He said it got up to 120 MPH. My HP reading was only 171.xx - That does not seem right to me at all. It may have been the trans slipping or something else. It could be correct, but I have some doubts. I don't know if the operator completely pressed the accellerator or if some other factor played in the low reading.
I will post the printout tomorrow, the graph looks good though it climbs steady and plateaus and keeps straight until you let off the accellerator.
Disappointing day to say the least